Case
History SeriesSmall Motor - Soft Foot Frame & Bearing Problem
I. BACKGROUND
The production personnel of a South Carolina chemical
company reported hearing a new noise emitting from a pump/motor
unit. Maintenance was dispatched to investigate the noise and
repair if necessary. The maintenance mechanic and electrician
assigned to the job requested vibration diagnostics to determine
the source of the noise and health of the machine.
II. CONCLUSIONS
A. A soft foot on the motor is warping the frame.
B. A bearing outer race defect exists at position
1.
III. RECOMMENDATIONS
A. While the motor is operating, loosen the foot hold-down bolt
on the southwest foot. The foot will rise due to the warped frame.
Temporarily (until scheduled shutdown) insert a shim the thickness
of the gap below the foot then retighten the bolt. At scheduled
shutdown, determine between sprung foot (as in Figure 1) and soft
foot. Soft foot will require proper shimming; sprung foot may
require milling.
B. During scheduled shutdown replace motor bearings.
C. During scheduled shutdown inspect the pump
base for evidence of settling.
Figure 1. Illustration of a sprung
foot
IV. DISCUSSION OF RESULTS
Manufactured by Reliance, the subject motor has an operating speed
of 3580 rpm, 25 HP, and is outfitted with NTN6310 rolling element
bearings. It is used to power the re-circulation pump for a 50%
caustic soda storage tank. The driven pump is a Durco I horizontal
centrifugal pump. Figure 2 is a sketch of the unit showing measurements
positions.
Figure 2. Horizontal centrifugal pump & motor
A. Warped Motor Frame
An
FFT analyzer was employed. The reading taken at position 2V showed
a peak at 2X line frequency (2FL). The peak clearly dominated
the spectrum with an amplitude of .5 ips (peak vibration).
Remember, "Concern should be given motors whose amplitude at twice
the line frequency (2 X 3600 cpm in the USA) exceeds approximately
.100 ips peak for in service motors… This would apply to
motors ranging in size from approximately 50 HP to 1000 HP"1.
Our analyzer showed five times .100 ips on a motor smaller than
50 HP (25 HP). The survey three weeks prior to the diagnostics
testing showed an amplitude of .305 ips or three times .100 ips
(the level at which we should give concern). See Figure 3. The
amplitude had increased 64% in just three weeks. A problem was
not only present, but also developing.
Figure
3. Spectrum showing high amplitude at 2X line frequency
Such high amplitude at this frequency might lead one to quickly
conclude that the motor is experiencing an electrical problem
because many electrical problems are associated with 2FL.
However, mechanical problems should also be considered when
motors show high amplitudes at 2FL.
It
is commonly agreed on that mechanical problems can cause high
amplitude at 2FL. A warped motor frame for example. The warp
can cause an uneven distance radialy between the rotor and the
stator’s magnetic field. At the location where the distance
is reduced due to the warp, a strong pull may occur relative to
the location where the distance is increased due to the warp.
Both events (strong pull/weak pull) happen every rotation of the
stator’s magnetic field. The stator’s magnetic field
rotates at the line frequency of 3600 cpm (in the USA) X 2 events
= 7200 cpm. The same frequency involved in many electrical problems,
yet in this case caused by a mechanical problem.
When the mechanic began to insert the shim under the southwest
foot (per recommendation 1 on page 1), he noticed a hairline
crack propagating from the southwest foot and extending to the
motor frame. The crack measured several inches in length. This
discovery added much weight to the conclusion that the motor
frame was warped and that the high amplitude 2FL was the vibration result generated
by the warp. A decision was then made to remove the motor, repair
the crack, determine between sprung and soft foot, and replace
the bearings. Figure 4 is a post repair picture of the hairline
motor frame crack.
Figure 4. Frame crack discovered on motor
(Photo taken after weld repair.)
The
mechanic determined that a soft foot coupled with improper shimming
twisted the frame and caused stress near the foot area. The stressed
area was acted on by high amplitude vibration and resulted in
the hairline crack.
B. Bearing Defect Outer race
To determine the source of the noise reported, previously taken
velocity and acceleration envelope measurements were examined.
Figure 5 is an acceleration envelope spectrum taken at position
1H. A band pass filter of 30k – 600k cpm was used to eliminate
rotational vibration. The resulting spectrum clearly displayed
multiples of BPFO indicating that a bearing problem existed.

Figure 5. Spectrum of Acceleration
Envelope Measurement position 1H
To
help determine the severity, the velocity spectrum (also previously)
taken at the same position was considered. A bearing defect of
moderate severity will usually display defect frequencies in the
velocity spectrum. Figure 6 is the velocity spectrum, which displays
many multiples of BPFO. A sideband cursor was placed over one
of the defect frequencies. Note that the delta of 10962 is very
near the BPFO fundamental defect frequency of 10920.
(BPFO=
3.07 X 3557 cpm running speed = the fundamental BPFO frequency
of 10920 cpm).
Figure
6. Spectrum of Velocity Measurement position 1H, showing many
multiples of BPFO
Having
so many multiples of BPFO, this spectrum fits the description
of a stage 3 bearing failure as described in the Technical Associates
Illustrated Vibration Diagnostic Wall Chart. It also indicates
that the source of the noise reported originates with the bearing
defect.
As
per recommendation 2 (on page 1), the motor bearings were replaced.
To confirm that a defect actually existed, the outboard (position
1) bearing was cut open and visually inspected. Figure 7 is a
picture of the outer race.
Figure 7. Outer race defect found at Position 1.
V. RESULTS OF CORRECTIVE ACTIONS
Motor repairs encompassed the welding of the frame crack, proper
shimming/alignment of the unit, and the replacement of the motor
bearings. A significant drop in amplitude at 2FL resulted from proper shimming/alignment,
and repair of the crack.
Compare
the before and after repair spectra in Figure 8.

Figure 8. Waterfall plot
displaying measurements taken before and after repair
The
amplitude at 2FL dropped from .305 ips to .026 ips (over 91%).
In addition, bearing frequencies disappeared.
Figure
9.
Acceleration envelope spectrum taken after motor repairs.
Note
that no bearing defect frequencies are present.
It
is understood that the motor continues to run with low to
moderate amplitudes of 2FL and no noises have been reported.
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